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HOT-48: Chief Scientist Report


Chief Scientist: L. TUPAS


Cruise Dates: July 24(test cruise); July 26 (aborted); 
              July 28 (aborted); July 31 (aborted)

Vessel: M/V Na'Ina (reclassified as a research vessel; 
        July 21 - August 1, 1993)

Operator: Auakewai Salvage, Diving, Fishing, Inc., Honolulu

Charter agreement with UH Marine Facility, Stan Winslow acting as
coordinator
 
Science Personnel:

Test Cruise: 	

Luis Tupas - UH Scientist, JGOFS, Chief Scientist
David Karl - UH Scientist, JGOFS
Dale Hebel - UH Scientist, JGOFS
Terrence Houlihan - UH Technician, JGOFS
Jef Snyder - UH Technician, WOCE
Richard Muller - UH Technician, HOT
Luigi Pozzi - UH Marine Facility, STAG
Jim Dorton - UH Marine Facility, STAG
Karin Bjorkmann - UH Visiting scientist
 

HOT-48:

Luis Tupas - UH Scientist, JGOFS
Dale Hebel - UH Scientist, JGOFS
Terrence Houlihan - UH Technician, JGOFS
Jef Snyder - UH Technician, WOCe
Richard Muller - UH Technician, HOT
Luigi Pozzi - UH Marine Facility, STAG
Jim Dorton - UH Marine Facility, STAG
Ricardo Letelier - UH Graduate Student
John Dore - UH Graduate Student
Sean Kennan - UH Graduate Student 




Daily Reports


July 21, 1993

M/V Na'Ina docks at UH Marine Facility, Snug Harbor to begin refit. A
portion of the starboard railing near the bulkhead had already been cut
off to provide an opening for the CTD trolley system.  At 1200, 3
laboratory vans were loaded on deck, as well as a trolley system for
the CTD package, a hydrowinch, a hydraulic power pack, and a rope
winch. The vans were mounted and welded onto pedestals at their
corners.  All the above items were welded onto the deck of the vessel.
Other pieces of equipment such as the spar buoys, floats, lead weights
and equipment boxes were loaded and secured to various places on the
ship.


July 22, 1993

Electronic and laboratory equipment were loaded into the vans.  Items
were moved around to make best use of the limited space available on
the ship.  Electrical power was supplied to the trolley system,
hydrowinch, rope winch and vans. Hydraulic and electrical components of
the hydrowinch were installed. It was planned to set sail the following
day for the test cruise, however, the hydrowinch was not completely
operational and no testing on it had been done, Additionally, a crutch
to support the crane while acting as a point of support for the
hydrowire had not yet been installed. Sailing day was set for July 24.


July 23, 1993

The hydrowinch was fully installed and tested. In addition, the vans
were chained to the pedestals they were mounted on. The CTD frame was
lowered over the side of the ship and the position of the crutch was
determined. The crutch was fabricated and installed. A series of tests
were made using the CTD frame to determine the best method to conduct a
safe deployment and retrieval.  I was satisfied with the results of the
tests and the final layout of the equipment on the ship. It was the
best we could do given the type of vessel we had to configure. I
scheduled departure time for the test cruise at 0800, July 24.


July 24, 1993

We departed at 0800 with all hands on board. The test site was 3 miles
off Barbers Point, Oahu where the bottom depth was about 800 fathoms.
The skies were overcast and it was raining, The remnants  of Tropical
Storm Doris was just crossing the Hawaiian Islands at this time. We
were experiencing 8 foot seas and strong winds. We arrived on site at
1000 and began a 500 pound weight cast to 1000 meters.  After the
weight cast, a series of frame "dunk" casts were conducted to work out
deployment and retrieval procedures and familiarize the personnel with
the operation. After the frame cast, we attempted to deploy the
sediment trap array from the stern. It was a difficult procedure under
the sea conditions we were experiencing and I decided to stop the
procedure after the weight and line had been paid out. Retrieval of the
complete package would have been very difficult under present
conditions. During this time, the CTD electronics and 3 bottles were
being assembled on the frame. A CTD cast was conducted to 250 meters
and some water was collected. Throughout all these operations the deck
was constantly awash and it was difficult to move about. We left the
test site at 1500 and arrived at Snug Harbor at 1700. Due to the
difficulties we experienced on board ship while trying to execute the
operations, as well as the presence of another storm system (Tropical
Storm Eugene), I decided to conduct HOT-48 on July 26.  The ship was
definitely not capable of sustaining the operations under the
conditions we experienced today.


July 25, 1993

A few additions to the ship were made. Chains were strung over the
railing and stern as a safety measure. Cleats were welded onto the deck
to provide support for the tag lines used during deployment and
retrieval of the CTD package. A plastic pipe was used to cover the
electrical wiring from the ship to the laboratory vans. Work vests were
borrowed from the R/V Kila.


July 26, 1993

I had scheduled sailing time at 0800. Upon arrival at Snug Harbor I was
told that the crew of the ship were being held at their office by the
US Coast Guard for  random drug tests. The crew finally did arrive and
we set sail with all hands at 1100.  We were experiencing 4 foot seas
and moderate winds on the leeward side of the island. We reached Kahe
station at 1400 and conducted the first CTD cast. During its retrieval
however, it was found that the hydrowinch could not bring the full
package (all 24 bottles filled with water) from the sea surface onto
the deck of the ship. Any attempt to lift the package out of the water
with the winch would result in the  package slipping back. The winch
would not even hold the package with its breaks when the package was
out of the water. We tried repeatedly to retrieve it using a
combination of the ship's crane and the winch. In the process the CTD
package hit the side of the ship and hung onto the deck of the ship
with the sampling bottles. We damaged 3 bottles in the  process. The
package was finally brought on deck but not without extreme effort and
considerable risk to the personnel. Sea conditions were relatively
mild  this day but I certainly would not do these operations again
under similar conditions.  After sea water samples were taken, I
decided to return to Snug Harbor and have the hydrowinch looked over
the following day.  We set sail for Honolulu at 1700 and arrived at
2030.



July 27, 1993

UH Marine Facility personnel looked the hydrowinch over. It was found
that the winch had to be in low gear to lift the package onto the ship.
Previous instructions to keep the winch in high gear throughout its
operation were not correct. The truth is, none of the marine center
STAG personnel were aware of the proper gearing of the winch.  I had
set sailing time at 1200 today but after checking the weather reports,
I decided to call today a weather day due to the presence of strong
winds (25 knots) and high seas (18 feet) at Station ALOHA.  In
retrospect, similar weather at Station ALOHA the previous day would
probably have forced us to return to Honolulu. Marine Facility
personnel raised the hydrowinch power pack onto stilts due to the
amount of wash on the deck each time we sailed. More lead weights were
loaded onto the ship to conduct a 1500 pound test weight cast. I
scheduled to set sail the following day.


July 28, 1993

We departed Snug Harbor at 0800 with all hands on board. We arrived at
Station Kahe at 1100 and commenced with a 1800 pound weight cast to
1000 meters. The hydrowinch was unable to maintain a winch rate of 60
meters per minute during the upcast at high gear. We had to switch to
low gear and maintain a speed of 35 meters per minute. This was not a
desirable speed but there was little we could do to improve it. After
the CTD cast, it was discovered that the heat exchanger of the
powerpack's cooling system was not attached. A cooling system using the
ship's seawater outlet (actually a fire hose outlet) was rigged to
provide coolant to the power pack. After  modifications to the power
pack were made we set sail for Station ALOHA. Weather reports from NOAA
showed high seas and strong winds in the channels and further north of
the island. I decided to continue towards ALOHA and assess the
situation once we were further north of the island. Sea conditions
worsened once we hit the channel and remained generally rough with
strong winds once we had gone past Kaena Point. We were experiencing
twelve foot waves and 25 knot winds gusting up to 30 knots. I decided
to stop the ship twelve miles northeast of Kaena Point and check wind
and sea conditions and determine if we could conduct CTD operations.
Floating arrays were already canceled. The rough and high seas combined
with the wind were totally unacceptable and beyond the safety standards
we had set. New weather reports showed that these conditions would
remain until Friday due to the presence of a high pressure system to
the north which was moving east. I decided to return to Honolulu to
wait out the bad weather.


July 29, 1993

HOT PI's (JGOFS and WOCE) held a meeting to assess the situation and
analyze weather reports at the UH Department of Meteorology. The high
pressure system was continuing westward and better weather was
predicted starting July 31. July 30 was to be called a weather day.
Sailing time was set for 0030 on July 31 and operations will be
restricted to CTD and water sampling. No biological experiments will be
conducted. All unnecessary equipment would be unloaded the following
day. Later in the afternoon, the HOT PI's individually received an
internal memo from the participating graduate students stating their
assessment and concern over safety aspects of the M/V Na'Ina and their
refusal to join the science party on the ship. Due to the lateness in
the day, HOT PI's were unable to meet to discuss the situation.
Discussions were set for the following day.


July 30, 1993

HOT PI's met at 0830 to assess the situation regarding the internal
memo addressed to them. The loss of 3 personnel from the science party
would make operations, even scaled down, more difficult. The memo
itself created anxiety among the science party which was already under
stress from the previous attempts at sea. Furthermore, the memo raised
the question of operational safety onboard the M/V Na'Ina based on
previous efforts to conduct CTD operations and the general outfit of
the ship. Although the HOT PI's believe that given good weather
conditions it would be possible to do a limited amount of work, a
decision was made to end the charter based on the increased liability
to the PI's for any mishap that could occur. UH Marine Facility was
informed of the decision and this was communicated to Auakewai.
Unloading of the ship commenced at 1000 and was completed at 1600.
HOT-48 was history.



General Summary and Assessment

The M/V Na'Ina severely limited the operational capability of the
program.  Even under ideal sea and weather conditions, only a limited
amount of work could be achieved. Unfortunately, weather conditions
during the period of the charter did not allow us to conduct even the
limited amount of work planned. The safety of the science party and the
equipment was my primary concern in all aspects of the cruise and at
all times. It was also the position of the HOT PI's that I be
conservative in my judgment of the situations we faced at sea. Despite
our efforts to prepare the vessel for oceanographic work, inherent
aspects of the ship compounded with equipment difficulties gave us very
little room for error and almost no flexibility.

It is unfortunate that our experience with the M/V Na'Ina had to be as
such.  It's use during HOT-21 was also unsuccessful. Based on that
experience, it was the position of the HOT PI's that the vessel was
unsuitable for oceanographic purposes. At that time, the ship was not
as well prepared for our kind of work.  Through unforeseen
circumstances, the program was left with no choice but to attempt a
cruise this year on the same vessel. JGOFS and WOCE personnel spent a
considerable amount of time (close to 2 months) planning this cruise
(HOT-48) and setting it up. It was hoped that the weather and sea
conditions during this summer would open up for us a window of
opportunity, however narrow, in which to conduct our research. We were
not that lucky.

A final comment on the safety aspect of this cruise. From the
standpoint of legality, the vessel had passed both US Coast Guard and
UNOLS safety standards specifically established for charter vessels.
The assessment of safety, however,  is also an operational parameter.
This parameter has to be assessed under the changing conditions of the
environment. What is operationally unsafe at one time would be
considered safe at another time. The use of the M/V Na'Ina restricted
the safety boundaries of operations. A good oceanographic vessel should
allow safe operations under a wide range of conditions. The M/V Na'Ina
was definitely not one and we should not convince ourselves that it
could be.